Our Thoughts and Remembrances

Image courtesy of Lil Doc's
From Roger Olsson:
From Reggie Kenner:
Mike was my hootch mate with Sgt Fritz, Terry Willman,
Swede, Mark Lenick,
maybe Griffith etc. He was a fun-loving guy with brown curly hair and a
little moustache.
He was from Detroit and proud of it judging by the way he talked.
Mike was very funny and he and his gunner Marvin Screen (Sweet Fat) were
quite a pair, full of fun and laughter. Funny how you could be laughing it
up right up until the mission was on, then right back to it over the smell
of JP-4 and oil while cleaning guns or post-flighting a huey.
Mike loved flying with the Lancers and along with Mr Sutton and Sweetfat,
they were a great crew.
I was on R&R to Sydney for a week and when I returned, I got the word that
there was a vacancy in the Hootch. Cox, Screen, Mr Sutton and Mr Hughes
had
gone down for some unexplained reason and crashed into a stream. I
wouldn't
be laughing with them anymore.
It was a war and we moved forward with the mission but there was a big
hole
in the hootch after Cox was gone...a big hole.
Info from the A/C database:
Accident Summary:
AIRCRAFT WAS NUMBER EIGHT IN A FLIGHT OF FOURTEEN. THE FLIGHT WAS ASSIGNED THE MISSION OF EXECUTING EIGHT COMBAT ASSAULTS IN SUPPORT OF THE 2ND BRIGADE. THE FIRST MISSION INVOLVED THE EXTRACTION OF ONE RIFLE COMPANY. THE FIRST SEVEN AIRCRAFT LANDED IN THE PICK UP ZONE AND DEPARTED WITHOUT INCIDENT. A LARGE TREE APPROXIMATELY 60 FEET TALL WAS DIRECTLY NORTH OF THE TOUCH DOWN POINT. EACH AIRCRAFT COMMANDER TURNED HIS AIRCRAFT APPROXIMATELY 20 DEGREES TO THE LEFT, WHICH ALLOWED SUFFICIENT CLEARANCE BETWEEN THE ROTOR DISC AND THE LARGE TREE, ALLOWING A SAFE DEPARTURE ON A NORTH NORTHWESTERLY HEADING. AIRCRAFT NUMBER 8, UPON APPROACH THE PICKUP ZONE, WAS INSTRUCTED TO UTILIZE A RIGHT DOWN WIND AND RIGHT BASE TRAFFIC PATTERN, DUE TO ARTILLERY FIRE IMPACTING SOUTHWEST OF THE PICKUP ZONE. BECAUSE OF INADEQUATE SPACING, RESULTING FROM THE CHANGE OF THE APPROACH PATTERN, THE AIRCRAFT COMMANDER EXECUTED A GO AROUND AND 360 DEGREE TURN TO THE WEST. THE SECOND APPROACH WAS SUCCESSFUL, AND THE LOADING OF FIVE PASSENGERS WAS ACCOMPLISHED. THE AIRCRAFT, UPON DEPARTURE FROM THE PICKUP ZONE, DID NOT EXECUTE A 20 DEGREE TURN TO THE LEFT, AND SUBSEQUENTLY FOLLOWED A FLIGHT PATH MORE NORTHERLY IN DIRECTION THAN THE PRECEEDING AIRCRAFT IN THE FLIGHT. AS THE AIRCRAFT EXECUTED A MAXIMUM PERFORMANCE TAKEOFF, THE MAIN ROTOR BLADES MADE CONTACT WITH A TREE, 60 FEET TALL, TEN INCHES IN DIAMETER, AND LOCATED 40 METERS FORWARD OF THE TAKEOFF POINT. IT IS SURMISED THAT THE AFOREMENTIONED BLADE STRIKE RESULTED IN AN INSTANTANEOUS DECAY OF ROTOR RPM TO A LEVEL UNACCEPTABLE FOR CONTINUED CLIMBOUT. THE AIRCRAFT THEN TURNED LEFT APPROXIMATELY 10 DEGREES, WITH A SLIGHT LOSS OF ALTITUDE, WHEREUPON THE UNDERSIDE OF THE AIRCRAFT AND THE TAIL BOOM PASSED THROUGH THE TOP OF A BUSHY DEAD TREE APPROXIMATELY 40 METERS ALONG THE FLIGHT PATH FROM THE POINT, THE LEFT SYCHRONIZED ELEVATOR WAS TORN FROM THE TAIL BOOM, AND REMAINED SUSPENDED IN THE UPPER LIMBS OF THE TREE. THE AIRCRAFT CONTINUED APPROXIMATELY 70 METERS ALONG ITS' FLIGHT PATH IN A NOSE LOW ATTITUDE, MAKING CONTACT WITH THE TOP OF THE JUNGLE CANOPY, DOWN THE SIDE OF A RAVINE, WITH THE FINAL POINT OF IMPACT BEING IN A STREAM 10 METERS WIDE, THE DEPTH OF THE WATER BEING APPROXIMATELY 4 FEET. FINAL IMPACT WAS IN A NOSE LOW ATTITUDE, WITH AN ESTIMATED 20 KTS FORWARD MOTION. UPON IMPACT, THE TRANSMISSION AND MAIN ROTOR SYSTEM WERE THROWN FORWARD, COLLAPSING THE CABIN ROOF, WITH THE ROTOR HEAD COMING TO REST IN THE PILOTS COMPARTMENT OF THE AIRCRAFT. THE CABIN PORTION WAS IMMEDIATELY ENGULFED IN FLAMES, AND AS A RESULT, ALL NINE PERSONNEL ABOARD PERISHED IN THE CRASH AND RESULTING FIRE.
And the Bn. logs of 3 September 1969 , provided by John Donaldson:
Hour
0657 Received call from Col. Sinclair: B Co. aircraft
went down
in PZ and was burning.
0705 D Co. advised that Redskin 36 reported the aircraft to
have
had a blade strike and exploded on impact. No knowledge of survivors
at this time.
0730 Received call from Lancer 3, Cpt. Rhodes: D/O on station,
security force in area, aircraft burning and ammo cooking off.
0745 From B Co. operations: Aircraft 537# AC Sutton; Pilot
WO-1
Hughes; Crew Chief SP4 Cox; Gunner SP4 Screen.
0755 From B Co.: CO and RTO, D/1/501 were on board aircraft
537#
0804 From Lancer 3: All personnel on board aircraft 537# KIA
confirmed by Brandy 63.
0822 Call from Col. Sinclair: Leaving accident area at this
time
and would like a report when all personnel have been extracted from
crash site.
0949 Col Kastner called to inform Maj Cone permission was
given to
blow aircraft 537# in place. Prior to destruction of aircraft all
bodies must be recovered and friendlies removed from area and
commander must give final clearance. (Col. Demming 1st Strike)
[end log entries concerning this incident]
It should be noted that the prior day the area was under a Phase I
Typhoon warning and all aircraft were grounded. There was damage to
buildings such as hangers but no aircraft were reported damaged.
Weather and winds were a factor the day of the crash and it is not
specifically known if wind gust played any part in the crash. Weather
was a serious factor for several weeks prior to and following the
crash.